Micro-foam drilling fluid
A drilling fluid and foam technology, applied in the field of drilling fluid, can solve the problems of complex drilling, not yet involved in the field of cementing quality, oil layer pollution, etc., to achieve the effect of reducing density, good oil layer protection effect, and eliminating leakage
- Summary
- Abstract
- Description
- Claims
- Application Information
AI Technical Summary
Problems solved by technology
Method used
Image
Examples
Embodiment 1
[0037] Tamuchage Oilfield belongs to the buried hill fault block oilfield. The Tongbomiao oil layer is mainly low-pressure, with well-developed micro-fractures and good permeability. Lost circulation is very easy to occur during drilling. In 2008, 4 wells lost circulation. The qualified rate of cementing is only 80%. We tested the micro-foam drilling fluid system in 3 wells in this block, and achieved remarkable results. The lost circulation rate was 0, the cementing quality rate was 100%, and the oil and gas layers were effectively protected. At the same time, the drilling fluid has an obvious effect in increasing the ROP.
[0038] In well Ta19-334-t209, after the second opening (300 meters) of well washing, the amphoteric ion polymer drilling fluid was used to drill, and the drilling fluid prepared by the method of indoor experiment (2) was added to the well depth of 900 meters, and at the same time Start all agitators and solid control equipment to increase the amount of g...
Embodiment 2
[0040] Well Xu 129-91 in Block Xu 211 was drilled to a depth of 1480 meters, and the drilling fluid prepared by the method of indoor experiment (2) was added, and the agitator and solid control equipment were started to increase the amount of gas mixing, so that the air bubbles were evenly mixed on the ground and circulated. After 2 weeks, the drilling fluid Marsh funnel has a viscosity of 61s and a density of 1.06-1.09g / cm 3 , the water supply of the mud pump is normal, the circulating pressure is reduced from 9.5MPa to 8.5MPa, the water loss is reduced from 4.8ml to 4.2ml, and other indicators meet the design requirements. The cementing quality is high-quality, the electric logging is successful once, the well diameter is regular, the tripping and tripping is smooth, and there is no jam display, and no short tripping operation has been performed in the whole well. It can be seen from the completion electrical logging curve that the amplitude difference of the micro-electrode...
PUM
Property | Measurement | Unit |
---|---|---|
Density | aaaaa | aaaaa |
Density | aaaaa | aaaaa |
Density | aaaaa | aaaaa |
Abstract
Description
Claims
Application Information
- R&D Engineer
- R&D Manager
- IP Professional
- Industry Leading Data Capabilities
- Powerful AI technology
- Patent DNA Extraction
Browse by: Latest US Patents, China's latest patents, Technical Efficacy Thesaurus, Application Domain, Technology Topic, Popular Technical Reports.
© 2024 PatSnap. All rights reserved.Legal|Privacy policy|Modern Slavery Act Transparency Statement|Sitemap|About US| Contact US: help@patsnap.com